AMA, Agricultural Mechanization in Asia, Africa and Latin America (AMA) (issn: 00845841) is a peer reviewed journal first published online after indexing scopus in 1982. AMA is published by Farm Machinery Industrial Research Corp and Shin-Norinsha Co. AMA publishes every subjects of general engineering and agricultural engineering.
AMA, Agricultural Mechanization in Asia, Africa and Latin America (ISSN: 00845841) is a peer-reviewed journal. The journal covers Agricultural and Biological Sciences and all sort of engineering topic. the journal's scopes are in the following fields but not limited to:
An improved Cassaba wear peeler was developed by modifying the existing Cassaba peeler. A comparative analysis was performed on the test results, and it was shown that there was a significant difference in the amount and quality of the peeled cassava between the existing friction peeling method and the improved method. The results showed that the improved machine performed well by giving a high rate of 75.4%, a throughput of 119 kg / h, a tuber meat loss of 5.88%, and a specific energy consumption of 57.1 kJ / kg. The average processing time of 17.5 minutes / batch and the cost of N6.25 / kg (1 $ US ≒ 360N) resulted in improvements of 42.3% and 26%, respectively. This improved technique eliminated the pretreatment work of trimming, sorting and sorting of Cassaba tubers, which characterizes other techniques. The operation requires little operator skill, is locally supplied with all the materials used in manufacturing, and can produce machines that are acceptable to the small processing industry.
Jackfruit is a fruit that many people like because of its sweetness, but it is one of the important unused fruits. Extensive research has been done on the added value of jackfruit, but the machining of jackfruit for separating bulbs remains of great interest. Therefore, in order to facilitate the extraction of bulbs, we have developed a semi-machining machine for removing the core of jackfruit and dividing the fruit. The test was carried out by processing fruits of three different lengths, small (15-30 cm), medium (30-45 cm) and large (45 cm or more), at different cutting speeds of 600,700,800 rpm. When operated at a cutting speed of 800 rpm with the developed machine, the core removal rate was 96%, 89.5%, 71.3% and the fruit damage rate was 12.2% for small, medium and large size fruits. It was 8.6% and 4.1%. The total time required to cut and separate the bulbs using the developed machine was 7.10, 10.0 and 12.4 minutes for small, medium and large fruits, 13.25, 18.07, and 27.20 minutes. Less than manual processing by experts. The throughput capacity of the machine for small, medium and large fruits was 66 kg / h, 114 kg / h and 144 kg / h, respectively. The total cost of the developed tool was about 20,000 rubies ($ 295) and the total operating cost was about 52 rubies ($ 0.77) per hour. The developed machine can be operated by the average person with minimal labor and is ideal for small to large processors and entrepreneurs.
The purpose of this study was to evaluate alternatives to reduce energy consumption applied to soil clearing. To do this, we developed an experimental device and evaluated the operation of the vibration-induced parameters. System integrated components for on-site evaluation: Frame tool carrier with introduction of three-point hitch and depth control mechanism system: Introduction of three sensors to measure tillage force, torque and frequency of subsoiler vibration Met. The oscillating impact force was applied through the rod and crank mechanism in the subsoiler whose motion was provided by the hydraulic motor. The device evaluation was complemented by a signal regulator and data collection system that allowed the registration of variables of interest such as system traction, penetration, applied torque and vibration velocity. The sensor calibration results showed a system correlation of 95% or more. In the field system verification at different speeds, amplitudes and depths of tillage, the traction force was reduced by up to 50% by using vibration-induced tillage compared to the non-vibration tillage state. This study showed a significant 33% increase in traction and torque magnitude when the working depth increased from 0.30 to 0.40 m. The traction force increased by 21% when the vibration amplitude decreased from 0.0707 to 0.060 m. No significant difference was found when the tractor velocity increased from 1.5 to 2.5 kmh -1. For future research, the device developed makes it possible to determine how tilling amplitude and working depth and vibration frequency affect traction in tilling work.
We designed and developed a front-mounted hydraulically driven cultivator in consideration of the negative traction force developed by the rotary cultivator and the traction capacity of the power cultivator. A suitable linkage system was designed and a cultivator was installed in front of the power cultivator. Field performance of power cultivators was measured with both front-mounted cultivators and rotary cultivators and with rotary cultivators only. These results show that the power cultivator has a 50% improvement in tillage performance index and soil when operated with a combination of front-mounted cultivator and rotary cultivator, compared to when operated with a rotary cultivator alone. Size and fuel consumption were shown to decrease significantly by 50% and 13%, respectively.
A manually operated regular row seeder for dry sowing of rice capable of planting two rows of rice at intervals of 25 cm x 25 cm was designed, manufactured and tested. The effective field capacity of the seeder was found to be 0.023 ha / h at a field efficiency of 47.38%, and the seeding rate was 10.1 kg / ha. Miss index, multiple index, and seed damage were 6.6%, 13.3%, and 2.1%, respectively. A comparative study was conducted to evaluate the performance of transplanting, spot seeding, and regular row seeding machines in the System of Rice Intensification (SRI). To sow on 1 hectare of land, the sowing machine required Rs.853 / ha (1US $ = 72Rs), which was less than manual transplanting and spot sowing in SRI. The developed seeder saved 66.7% and 72.4% cost compared to manual transplantation and spot seeding.